Page 318 - 360.revista de Alta Velocidad - Nº 5
P. 318

Sol-Sánchez, Miguel. Moreno-Navarro, Fernando. Rubio-Gámez, Mª Carmen.




                 of 250 mm. The height of the ballast layer was 300 mm under the sleeper, which is a common
                 value found in railway tracks, and allows for maintenance tasks (UIC Code 719-1). The ballast
                 used  in  this  study  was  composed  of  ophite,  with  appropriate  size  (mainly  between  63  mm
                 and 31.5 mm, EN 933-1) and resistance to fragmentation (lower than 8%, EN 1097-2) for its
                 application in railway tracks according to EN 13450, as well as the rest of properties were in
                 consonance with such Standard.
                       2.2     Test procedure


                 In order to prove the efficiency of the proposed technique (stone-rubber blowing) to reduce the
                 railway track maintenance, the testing plan included the analysis of the behaviour of a track
                 section reproduced in laboratory when different solutions are carried out as maintenance for re-
                 leveling after ballast settlement. These solutions were: stoneblowing process as conventional
                 maintenance technique; stoneblowing combined with the application of different USPs used
                 as rseference elastic element; and the incorporation of diverse quantities of rubber particles
                 (10%, 25% and 50% over the total volume of the mix of particles blown) used to replace part
                 of the small stones during stoneblowing process (stone-rubber blowing technique). Figure 2
                 represents the scheme of the different solutions applied.






































                                                       Figure 2. Testing plan.

                 For this study, a series of dynamic tests were carried out in order to reproduce track section
                 settlement, and then, to simulate maintenance techniques (conventional stoneblowing as
                 well  as  the  combination  of  this  process  with  the  incorporation  of  elastic  elements)  for
                 analysing the effect of each solution on track section behavior. The dynamic test consisted
                 of applying 200,000 loading cycles at 4Hz of frequency with a maximum stress over the
                 ballast surface around 250 kPa. These loading conditions are considered appropriate for
                 simulating the effects of passing trains (Indraratna et al., 2006; Bach, 2013; Sol-Sánchez,




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